Bellows and Bellows Fabric etc.
I used medium density fibre (MDF) boards of various thicknesses for the bellows
boards and the wind chest. It's flat and stable (and I had it in the waste
box anyway). As long as you regard it as fairly stiff cardboard and amend
your woodworking techniques to accommodate this fact its ok. In Australia
(and no doubt in the rest of the world too) there are now available fast
helix narrow shanked 'man made timber' wood screws. They work well into MDF
as long as you don't overtighten them and strip the hole. If it's a critical
or load bearing screw I try to back the MDF with a bit of proper timber and
screw clean through into that. I seal the surfaces and cut edges with shellac
or sanding sealer. Both of these sealing methods present problems if you
have to glue onto the sealed surface later and you will have to abrade the
surface with glass paper to destroy the sealed surface and get to the fibres
below.
The traditionalist in me thought leather bellow fabric would be 'pukker'.
Unfortunately the combined thicknesses of the folded leather prevented the
bellows from closing to the 1/4" required and hence the throw of the crankshaft
(7/8" crank) became too great and the crank would not go over 'top-dead-centre'.
The solutions were to remake the bellows with rubberised fabric (too many
hours - and I had almost got an airtight seal on the system) or remake the
crank shaft. I chose the latter (two and a half hours work) and opted
for a 17mm crank ie 34mm (1 5/16") from fully closed to fully open. I hope
it will generate enough air volume from this reduced throw. Time alone
will tell. Another minor problem I have created is that I backed up
my leather flap valves with thin MDF to keep them flat. They work like a
treat but the air system now has a distinct 'clap, clap, clap' as the various
valves seal. The motto there is 'Do it like the book says'.
Bellows and Air Sealing
When joining of the two bellows 'side by side' it is very difficult to get
an air seal. I put a shim rubber rectangular gasket (this is sometimes called
gasket rubber or insertion rubber) between the edges of the top boards of
the bellows (after gluing them side be side) and the air reservoir. The gasket
had an additional strip running down the length of the joined area and the
whole system was set in clear silicon sealant (CSS). The air reservoir
was then set onto the gasket with CSS and screws. Even so the system leaked
like a sieve. Eventually I used CSS in every nook and cranny and the system
became reasonably air tight.
If I ever have to make paired (or multiple) bellows again I would consider
making them individually and them sticking them onto a thin intermediate
board. They would then be flat and probably air tight. The 6mm MDF wind chest
was pinned (12mm pins) and PVA glued together. When the glue was dry all
joints had a fillet of CSS squidged into them with a finger tip. I attempted
to make an air seal around the take up drum drive shaft by forcing the shaft
through a patch of 1mm shim rubber which was stuck over the bearing block
and bearing hole. The Jury is out on this one as the wind chest is still
leaking from somewhere.
The inspection window in the lid of the wind chest is 5mm Perspex/Lucite.
It was cut about 12 mm oversize on the width, set on contact adhesive and
again received a fillet of CSS. The lid seal is a 'Raven' brand hollow 'D'
section draught excluder strip of about 6mm uncompressed height. I set the
hinges to give a compression to about 2mm and I cant detect any air leak.
(There is one but I don't think it's from that seal). If using a hollow section
seal on the lid don't cut right through it when you cut the mitres as it
will leak. Leaving about 3mm in the corner of the mitre seems to stop this.
The Drive Mechanism
I made each of the wooden wheels from a pair of discs of 1.7mm thickness
ply which were glued at the centre and then turned to size 'on the shaft'.
Since the disks were not glued to the edge it was relatively easy to groove
round the perimeter with a rat tailed file. Amazingly the local vacuum cleaner
store had the rubber drive belt specified. The first 18mm wheel can easily
be made from painter's masking tape wound onto the shaft as it is turned.
Tuning for the correct ratio is a matter of adding or reducing turns and
it is dead easy to change diameter. It doesn't need the layer of abrasive
paper to be added as it has an inherent friction.
The cranked con-rods were each band sawn out of a 10mm hard wood board (I
finished by making half a dozen until I got the length and shape I needed)
and the connection to the bellows was through a 4mm hole drilled in the bottom
end of the rod via a 4mm 'L' shaped rod. This was screwed on below the bellows
and allowed the con-rod to rock freely to and fro as the crank went through
its 360 degree rotation.
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